Smashing through the track buffers, the express careered across the station concourse, broke through the station wall, and crashed to the street below, where it remained for four days drawing crowds of curious onlookers.
On 22 October 1895, the Granville to Paris and Montparnasse express, operated by Chemins de fer de l'Ouest, was made up of steam locomotive No. 721 (a type 2-4-0, French notation 120) hauling three luggage vans, a post van, and six passenger coaches. The train had left Granville on time at 08:45, but was several minutes late as it approached its Paris Montparnasse terminus with 131 passengers on board. In an effort to make up lost time, the train approached the station too fast, at a speed of 40–60 km/h (25–37 mph), while there was a failure to apply the Westinghouse air brake. Without sufficient braking, the momentum of the train carried it slowly into the buffers, and the locomotive crossed the almost 30-metre (98 ft) wide station concourse, crashing through a 60-centimetre (24 in) thick wall, before falling onto the Place de Rennes 10 metres (33 ft) below, where it stood on its nose. A woman in the street below was killed by falling masonry, and two passengers, the fireman, two guards and a passerby in the street sustained injuries.
The woman, Marie-Augustine Aguilard, had been standing in for her husband, a newspaper vendor, while he went to collect the evening newspapers.
The locomotive driver was sentenced to two months in prison and fined 50 francs for approaching the station too fast. One of the guards was fined 25 francs as he had been preoccupied with paperwork and failed to apply the handbrake.
The railway company settled with the family of the deceased woman, and arranged for the education of her two young children, as well as proposing future employment for them.
The passenger carriages were undamaged and were easily removed. It took 48 hours before the legal process and investigation allowed the railway to start removing the locomotive and tender. An attempt was made to move the locomotive with 14 horses, but this failed. A 250 tonne winch, with 10 men, first lowered the locomotive to the ground and then lifted the tender back into the station. When the locomotive reached the railway workshops it was found to have suffered little damage
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